Eduardo's 94 Mustang GT thread
Small update
Fixed the bad caliper a few months ago. Still need to replace the dry rotted rear tires and recharge the a/c refrigerant. Car hasn't been moved at all for almost three years.
Last edited by edumspeed; Jun 1, 2017 at 06:31 PM.
New edge brakes.
Those twin piston calipers made a huge difference on the car. Very good feel and awesome stopping power over the stockers. Can't wait to later put hawk brake pads
The lancer has hawk OES pads and felt better than OEM, so the hps or hps 5.0 should be even better for the mustang.
The lancer has hawk OES pads and felt better than OEM, so the hps or hps 5.0 should be even better for the mustang.
Been driving the Mustang these past weeks and has worked pretty well. Just had the drivers side window mechanism locked itself on the down position without any aparent reason once. Was a PITA to get the window motor out with the glass down. The motor was ok. I gave the glass a nudge and got it loose. It has been working well ever since 
Just this morning I recharged the a/c with some refrigerant and it's working as cold as it was before. No more foggy glass during the rain or getting swamp *** in this hot weather lol.
I'm also trying to stop the rust from spreading even more. Applied some goo on the top to try it out.

Just this morning I recharged the a/c with some refrigerant and it's working as cold as it was before. No more foggy glass during the rain or getting swamp *** in this hot weather lol.
I'm also trying to stop the rust from spreading even more. Applied some goo on the top to try it out.
Last edited by edumspeed; Jun 1, 2017 at 06:29 PM.
Update
Been using the 94 as a daily for two months now and has been doing good so far. But as you may know with old cars something will always fail. Yesterday morning I started it up as normal an a burnt wire odor surfaced. Noticed my car phone charger wasn't lit so i pulled it out. The thing roasted itself. Went on my way and found out there were no turn signals either. Today I replaced a 15 amp fuse and that solved the problem. Or so I thought. No turn signals again
When I get out of my doctor's appointment I'll check this thing. No idea wtf is going on.

Edit: Fixed the issue. It was something that fell into the cig lighter and was causing a short.
When I get out of my doctor's appointment I'll check this thing. No idea wtf is going on.
Edit: Fixed the issue. It was something that fell into the cig lighter and was causing a short.
Last edited by edumspeed; Jan 14, 2018 at 08:00 PM.
Not so good update
That happened on November 18th 2017. I managed to fire it up and took me home. Bad news is that I spent an entire week drying it up and cleaning the inside. And the transmission is busted. Got water inside and damaged the already slipping clutch packs. Only two foward gears work and reverse. And has a nasty short that drains the battery. I'm seriously thinking of parting it out as a donor for a 95 v6 i got to see and can get dirt cheap. Or do a T5 swap or sell it to someone else and get something newer.
Mustang stays... for now.
Thankfully the guy never replied back, and I'm glad since he was lowballiing me for just offering $600 for it
Got another new starter thanks to lifetime warranty @ pepboys lol. It fired right up. Vroom vroom



