SN95 Mustang 1994-2004 Mustangs Member Tech & Restoration Discussion

Eduardo's 94 Mustang GT thread

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Old 12/22/14, 01:54 PM
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Clean and with a nice coat of paint


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Still need 99-04 brake pads. A pitty that the 94 spec ones are like new

Last edited by edumspeed; 12/22/14 at 01:56 PM.
Old 12/22/14, 01:56 PM
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Originally Posted by edumspeed
Clean and with a nice coat of paint
Nice. Always easier when they're off the car!
Old 12/22/14, 01:59 PM
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Found a pic on an article about the swap on where the spindle needs to be grinded for the calipers to fit. Red line where there's interference and blue line the material to be cut.

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Old 12/22/14, 02:00 PM
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Originally Posted by laserred38

Nice. Always easier when they're off the car!
Ya. Too bad the rears are still in the car lol.
Old 8/27/15, 10:40 PM
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update

Ordered a head gasket set because most probably one of the head gaskets was incorrectly installed and is causing the weird symptoms the motor has. And also I scored this:



Old 8/29/15, 12:27 PM
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nice score!
Old 8/31/15, 02:20 PM
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Originally Posted by StangMahn
nice score!
Yeah. I couldn't believe myself. Asking price was $80 and I made a $50 offer for kicks and the guy accepted it

Last edited by edumspeed; 9/1/15 at 03:15 PM.
Old 8/31/15, 02:22 PM
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Gaskets and arp ultra torque lube arrived today. Teardown begins tomorrow
Old 9/1/15, 03:02 PM
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I made some good progress today. Just need to remove the headers and valve covers to unbolt the heads off the block. Then the long proces of cleaning the mating surfaces an re-assemble everything back.


Last edited by edumspeed; 9/4/15 at 05:14 PM.
Old 9/1/15, 03:13 PM
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side note:

Driver's side caliper is bad. Wheel gets locked
Old 9/2/15, 09:46 AM
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Driver's side head is out.

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Old 9/2/15, 09:57 AM
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This is a rough idea of how I want the car to look in the long run.
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Old 9/2/15, 12:36 PM
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Found the cause of the cooling & pinging issues

Last edited by edumspeed; 9/4/15 at 05:05 PM.
Old 9/4/15, 05:10 PM
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Cylinder heads and rockers are installed. I also got rid of the thermactor tubes that were doing nothing. I just cut the metal tubes from the junctions on the heads and flipped them. And for sealing them, i used a section from the discarded head gaskets
It's a shame I'm broke atm so I couldn't replace them with roller rockers
Old 9/8/15, 06:29 PM
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is that a garret turbo??? would love to see the numbers on it!
Old 9/26/15, 10:22 PM
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Originally Posted by Jim74656
is that a garret turbo??? would love to see the numbers on it!
Seller never shipped it. I oppened a case and was given a refund.
Old 9/26/15, 10:27 PM
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Update

Fired up the engine. There's white smoke and an oily residue from the passenger side exhaust (where the gasket was installed incorrectly) and isn't idling right. Pretty frustrated right now.

And the shift kit arrived today.

Last edited by edumspeed; 10/12/15 at 08:18 AM.
Old 10/12/15, 08:17 AM
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I went at the car again and figured out the unsteady idle it had. The vacum hose junction below the alternator was unhooked and the egr and fpr hoses were mixed up. Now it purrs like a big kitten lol. The oil getting off the passenger tailpipe is still an issue, but since I put 5w30 oil in the crankcase and the piston rings must have suffered a bit for the head gasket issue must be going past them. I'll just put 20w50 oil as it had that on the begining.
Old 10/13/15, 12:01 PM
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Originally Posted by edumspeed
This is a rough idea of how I want the car to look in the long run.
Sweet.
Old 10/20/15, 08:08 AM
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Nice
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